- The Master and Chief Engineer both entered guilty pleas in the Tauranga District Court on 10 Sep. after admitting charges relating to grounding of the log-carrier MV Funing.
- They were fined $3250.00 and ordered to pay $130.00 court costs.
- The engine failure was the cause of the issue.
- It was later proved that the master was aware of the issue with the main engine prior to departure and failed to notify the Pilot that there was a problem.
- The Chief Engineer was also proven to have failed to retest the main engine.
Master Liang Guang Hong and Chief Engineer Chameekara Prasad Nanayakkara of the log-carrier MV Funing, have today been sentenced and fined after admitting charges relating to the grounding of the ship at the Port of Tauranga, says an article published by Scoop.
Charges filed against the Master
This followed an investigation by Maritime NZ after the Singapore-registered ship lost power and passed over a channel marker with the propeller becoming caught in the marker chain, before making contact with a sand bar in the Tauranga Harbour channel.
The Master was fined $3250.00 and ordered to pay $130.00 court costs, after pleading guilty to one charge, of operating the vessel “in a manner which caused unnecessary danger or risk to other persons or property, including the passengers and crew of the MV Funing.
Charges filed against the Chief Engineer
The Chief Engineer also admitted one charge under section 65(2)(a) of the MTA, for causing or permitting the ship to be “operated, maintained, or serviced, in a manner that caused unnecessary danger or risk to any other persons or property, including the passengers and crew of the MV Funing”. He was also fined $3250 and ordered to pay $130 court costs.
The maximum penalty for both charges was 12 months’ imprisonment or a $10,000 fine.
How it all started
“The problem started when one of the engine’s fuel quantity pistons indicated an error, which means that if this isn’t addressed, the engine’s power will be reduced – which is the power it needs when exiting the narrow harbor entrance.”
In the hours leading up to the engine failure, the Chief Engineer tested the affected parts a number of times, each time triggering an alarm suggesting the problem had not been rectified.
“The Pilot subsequently came aboard around midnight and the master handed him the Pilot Card which indicated that there were no issues affecting a safe departure.
But as the ship tried to increase speed on leaving Port, the Chief Engineer realized there was still a problem with one of the fuel quantity pistons and that the engine was not responding with the shift to ‘full ahead’ (full power).
The Pilot asked the Master several times why the ship was going slowly but did not receive a clear explanation,” Mr. Abbott said.
As a result, the No. 2 engine cylinder lost all power, and during this time the wind and swell had increased. At 0043 hours the Pilot called the tug boats to come and assist and the Master ordered the anchor to be dropped. At 0047 hours the main engine stopped after the propeller became entangled with the channel marker while the stern swung around and came into contact with the sandbank.
“The tugs then turned the vessel into the deeper channel water and held it there until it could be towed into the safer anchorage.”
The Master was aware of the issue all along
Mr. Abbott said the Maritime investigation and subsequent prosecution proved that the Master knew there was an issue with the main engine prior to departure and failed to notify the Pilot that there was a problem.
The Chief Engineer was also proven to have failed to retest the main engine to ensure it was operating on all 5 cylinders after attending to the fuel quantity piston error.
The Funing is currently being towed back to Singapore which is expected to take around 40 days.
Did you subscribe to our daily newsletter?
It’s Free! Click here to Subscribe!